26 April
|
The brake master cylinders have now been ‘bench bled’ (though without
removing them), and the feel is much better. I’ve dispensed with the three
individual fluid reservoirs. They were prone to leakage and made access to
the master cylinders difficult. I now have a single reservoir bolted to the
back of the wheelarch.
The carburettor’s been stripped and cleaned, air passages and jets
blown through, though with no obvious fault spotted. I measured jet sizes and
replaced one of the primary jets with one from my tuning kit which better
matched the size of the other. I’ve also measured all plug lead resistances
and re-checked coil resistances, etc. and found no fault. I’ll have another
go at running the motor next week and see if I can narrow anything down.
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01 May
|
Made some passenger seat supports from aluminium channel, and also
cut some for the MX5 seats. I’ve been trying to find a way of not drilling
additional holes in the floor for the MX5 seats, but think this is going to
defeat me.
Gerry’s header tank and support bracket delivered. The bracket mounts
it a couple of inches too low – it needs to be the highest point in the
system. A couple of plates can be made out of aluminium to raise it up to the
level where the previous tank was mounted. Other than that, the Rover top
hose can be cut in two to fit both into and out of the header tank. The fan
thermoswitch, I now realise, screws into the boss at the top of the radiator.
All in all, the cooling system is simplified with fewer joints.
I’ve fitted a valve in the fuel tank vent, one that operates both
ways at a small pressure. This should help to stop the fuel smell, but was a
bit expensive.
At last a communication from Speedy Cables to say the speedometer
should be ready by the end of next week. They really haven’t lived up to
their name, this was sent to them on 21st February!
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04 May
|
The engine’s been running again (after replacing a blown diode
bridge). No sign of the previous misfire, but still a lot of top-end clatter
to be investigated. Cooling system almost completely continent! The dwell’s
checked OK at around 35 degrees.
Checked the wipers with the engine running – unfortunately the fast
speed isn’t sufficiently faster than the slow speed to comply with IVA
requirements, so I’ve ordered a new motor. I’ve also ordered some switch
identification stickers.
Spent some time making seat brackets to adapt the MX-5 seats. The
seats sit very low and are compliant with IVA requirements for seat belt
height with a good margin – nearly 2 inches!
More time spent bleeding the brakes. Hopefully getting a bit less
spongy.
|
13 May
|
Fitted the new wiper motor, notable increase in speeds, though not
yet checked frequency. Speedometer received back, calibrated, and fitted.
Spent a bit of time tidying under the bonnet, and some time on seat frames
and locations to aid transfer of the MX-5 seats.
The fuel pressure gauge doesn’t work properly despite now being
correctly wired. It really needs some advanced diagnostics, though currently
I’m suspecting the sender unit. It seems to give an output voltage of around
200mV when the fuel pump’s on, which sounds much too low.
I’ve been filling in forms and collating paperwork in preparation for
sending off with the IVA application. Probably do this when I’m back from
holiday in a couple of weeks. There’s really not too much left to do on the
car.
|
10 June
|
Big step forward is I submitted the IVA test application a week ago.
This coming Saturday I’m trailering the car to my MoT garage for a sort of
pre-MoT and to help me balance the brakes. Worked out I needed to trailer the
car around six times (maybe more) so in the absence of a very local hirer
I’ve bought secondhand a neat Brian James four-wheel trailer which fits in the garage.
I’ve spent a bit of time ‘snagging’ and getting things in order for
the test, ensuring all wiring’s covered in convoluted conduit, bolts are
sticking through nuts properly, and pipes and wiring are well supported. I’ve
also obtained a new timing light and gastester to replace my 30-year-old ones
which didn’t work any more! I’ve
adjusted the timing to 10 degrees BTDC static, vacuum advance disconnected. I
think this is a reasonable starting point. I’ve adjusted the carburettor to
give CO levels of around 3% which is well within the allowable for the age of
engine.
I’ve started to cut out footwell carpets from a roll I got cheap at a
local autojumble. Although patterns are now made for my own, I’m not
confident of them being finished before IVA test time.
Still some niggles – the engine rattle being the largest, sounds
tappety but I’ll get a view from Andy at Grappenhall Motors on Saturday. Not
yet fixed the fuel pressure gauge, though I’m suspecting a faulty sender
unit, and the float on my fuel gauge sender has sunk! I’ve sent for a brass
replacement from Moss.
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05 July
|
The ’pre MoT’ was a proper MoT – which I failed on brakes, rear brake
and handbrake efficiency too low. The trip also revealed some persistent
clutch drag which caused dome difficulty engaging first and reverse. A second
visit with tightened handbrake didn’t turn out much better. I puzzled over it
for a while – then realised I’d been misled into believing I needed a strong
bias towards the front brakes. The set up I’ve got is MGB – the original MGB
had single-line hydraulics, with no pressure limiting valve, so the balance
bar setup should be 50:50 front to rear. However, my Hawk has a little more
rearward weight bias, and has high friction (Greenstuff) front pads –so I
need a little bias to the rear – not too much, which would upset the IVA.
I’ve gone back to first principles to calculate the setup – I may
send this to Phil to see if he thinks it’s worth publishing.
I swapped the 0.7” master cylinder on the rear brake line with the
0.625” clutch master cylinder, and adjusted the balance bar to give
approximately 53% bias to the rear brakes. This solved both problems – the
clutch operating lever has more stroke and now allows quiet and easy
engagement of all gears, and the brakes passed the MoT today!
Rear drums have been drilled with inspection holes in case the IVA
people are applying the letter of the regulations.
The MoT emissions test showed that somehow my CO emissions were less
than 1%. So much for the Gastester. I increased them to a healthier 3%!
I’ve spent some time with carpets to make the interior look a bit
presentable while I wait for Gerry’s carpet set to be produced, though
there’s a bit more to do. I’ve sorted the fuel gauge with a new float. I’ve
tidied up a number of loose ends in advance of the IVA test – which is booked
for 8:00 on 23 July.
|
Sunday, 6 July 2014
Towards the MoT
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